Recently, the heat wave at the production site of Xiangshan Cement Rory Branch has surged. The problems such as large deviation fluctuation of roll gap and material leakage at the edge of roller directly affect the operation efficiency and energy consumption index. Faced with this challenge, the branch quickly set up a technical research team to discuss and formulate a maintenance plan overnight, and a battle for independent maintenance with high temperature and time began. In

three days, five maintenance workers volunteered to plunge into the equipment area of nearly 40 degrees Celsius. Beads of sweat hung on the forehead under the helmet, dark salt stains on the back of the work clothes, and the sound of gloves rubbing against tools mixed with the roar of the equipment running became the hottest footnotes of this summer. "Outsourcing maintenance cycle is long, we do it ourselves, we can not only seize the time, but also save the cost!" Worker Lao Wang's words expressed the consensus of the team. Disassemble the old and install the new, calibrate and debug, seal and reinforce.. Every step is a precise benchmarking scheme, and every screw is firmly screwed in place. When the last set of bolts was tightened and the equipment restarted, the steady buzz made everyone breathe sigh of relief-this "autonomous war" was effective!
"Xiangshan people" in the face of the "baking" test, they regard the high temperature as a "touchstone": sweat drips down the helmet belt, evaporates instantly on the surface of the hot equipment, but condenses into a more firm responsibility in everyone's heart; during the maintenance interval, someone picks up a mouthful of cold water, wipes his face and climbs up the equipment; The technical backbone squatted beside him and explained the main points to the novice while measuring the data. "If the equipment is stable, you will feel at ease when you sleep at night!" Young worker Xiao Zhang's words are simple but powerful. Over the past few days, the overhaul has achieved immediate results. The current of the circulating bucket has been reduced by more than 10 A, the production of Taiwan has been steadily increased by 5-8 tons/hour, and the power consumption of the cement process has been reduced by 0.4 kWh/ton. The replacement of the feeding device, which was completed completely independently, directly saved the cost of outsourcing by about 55000 yuan.
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